Week of April 29, 2012 18 hours. I worked alone this week and I am not sure where the time went. I ordered more tubing for the fuel pump (this is a FI plane so the pump and filter require some well bent tubing in the cabin). I “practiced” on my last piece, which is to say, I bent it but the outcome was less than ideal – however, it was better than the piece that was in there. This step was largely done 6 weeks or so ago. Last week Steve and I tried to put the doghouse on the fuel pump and it wouldn’t fit. The solution was complicated but involved moving the pump aft an inch or so and the filter aft about half that amount. That meant nothing fit any more. The tubing arrived Thursday and I plan to bend it next week. Practice is helping! And it damn well better – I’ve spent $70 on extra tubing.
Next, at Vlad’s urging I worked on getting the engine mount on. Well, the engine mount is pretty easy – if you discount how hard drilling those 6 holes is. Four of them go through the stainless steel firewall (really hard), then a thick aluminum fitting (easy drilling), and then through steel. The other two just go through stainless steel and aluminum. Each hole took close to 20 minutes to drill – and that was after buy new TiN coated bits at Home Depot for $8 each. But before putting the engine mount on I needed to construct the battery box, mount it and then mount two electrical relays. The relays are really simple to mount – just four bolts that go into 4 platenuts, There’s a backer plate to build and four or five rivets to drill out. I’m 99% sure Van’s sent the wrong platenuts – right size but wrong threads. I utterly stripped one bolt trying to get it in. So after riveting this all together I got to take it apart and re-do it with the platenuts (K-1000-32) that were threaded like the AN-4 bolts. All-in-all it was a 2.5 hour job that took 6 hours…a lot of sweat and a few choice words.
Drilling the engine mount on was pretty straight forward. I used my engine hoist to locate it and then drilled it in place. I have not torqued the bolts yet as there several holes I need to drill through the firewall for the throttle, mixture, prop control, and heat. Plus I need to build the heat control box. Torquing the bolts shouldn’t take long.
Next week I want to get the canopy mounted to the frame. I’ll need warm sunny weather so I can work on the patio and keep the plexiglass warm to keep it from cracking. I’m not sure how long this will take as I need to cut the plexiglass some more, and there are skirts to make and install. I’m guessing it will take more than a week to do this step. Future steps will include bending the fuel pump tubing, cutting the holes in the firewall, re-installing the rudder pedals, and putting the plane on gear.
Week of April 22, 2012 32 hours. Steve came back and it was one of our less productive weeks, mostly because I was so tied up with other business – work and fly-in related things. We did get the canopy frame mounted to the plane, I trimmed the tracks on the aft end, and we mounted the center track on the turtle deck. Every step seemed to be fraught with problems that needed to be fixed before going on to the next step.
After measuring and debating how to square the rails we started bolting them to the fuselage per the plans. Getting the washers and nuts on was a problem because they were located at the edge of a channel and there was no straight in access. Eventually I wised up and relieved the area under the bolts (screws?) so I had a straight up access. After hours of sweating each washer and nut, the process got much faster and was a one man game not requiring four hands. A hint in the plans would have been nice.
Next we mounded the frame and when sliding it aft, it did not quite clear the turtle deck on the right (pax) side and was just touching on the left (pilot) side. We dug out the bending jig/form and rebent the frame so it would clear. Doing that caused the front bow to expand too. With a wider front bow the wheels would jump out of the track at the aft end where I’d ground the tracks to prevent them from overhanging the side. Hmmm. That initially seemed to be a fatal error calling for replacement tracks. It occurred to me if the wheels rolled down the center of the tracks, without outward pressure, they would stay in place. Bending the front bow a tad narrower made the aft bow narrower and we were back with the aft bow hitting the turtle deck. Agggghhhh.
Well the solution was pretty obvious and a trip to the aviation aisle at Home Depot yielded pipes for my pipe clamps (purchased after Steve’s last visit). We came back and clamped the front bow to hold it at the narrow end of what worked in the tracks and then we bent the aft bow out. The clearance right now is almost zero but the plans do say the plexiglass will spread the frame about 1/2 an inch, which should provide plenty of clearance.
We would have done more but I was disorganized, had to work one day, and Saturday and Sunday were devoted to hosting RV-1 and the Regional Festival of Flight at Suffolk air port. Late Friday afternoon Vlad Karpayov arrived from New Jersey (practically NY) in his RV-9A. Vlad flew Steve to Suffolk Saturday morning and let me fly back Saturday evening. Sunday was a fairly miserable day weather wise and we canned our plans to go to Suffolk. Around 11 am the ceilings lifted enough for Vlad and I to fly. I got a total of 1.7 hours and 3 take-offs and landings in his 9A. I owe Vlad a debt of thanks for sure. He was very generous with his plane, his time, and his advice. All I can say is the 9 is an absolutely awesome plane to fly and I need to get mine done.






















